With everything assembled, and with TomB engineering’s assistance, it was finally time to see if the engine would start.
The engine was checked over and all the torque settings were confirmed. For the heads this meant an initial tightening followed by a final tightening when the manifold had been bolted on.
The engine was mounted up to a refurbished gear box I’d acquired earlier, along with a starter motor that was sold-as-seen. With no clutch between the gearbox input splines and the engine flywheel this mean that the starter motor would be able to turn the engine over without driving the gearbox. With the wiring loom attached to provide power to the ignition and fuel pump, the coil and HT leads in place to provide juice to the spark plugs and a battery wired up to the starter and earthed to the gearbox it was ready to go.
The initial push of the ignition button was rewarded by a click and whirr from the starter motor, so at least that was good. The ignition is the same 123 unit fitted to Judith so the indicator light showed that it was powered and the timing could be set. However, the fuel pump wasn’t priming. Once we’d worked it out it was obvious: the loom had no earth – when it’s in the car it has all sorts of earths that make their way back to the gearbox but that was missing here. One fly lead later and the fuel pump primed and filled the carburettor.
Now we were ready to go again but the battery was now flat from turning over the engine whilst we were trying to diagnose the fuel pump’s missing earth – the starter would click but not whirr. Running jump cables from Lotte gave us the power we needed and, after a few seconds it caught! It ran for about 20s before starting to die and I cut the ignition. Still, that’s pretty impressive given the choke and throttle were set at about half as a guess – some dynamic adjustment of them could probably have kept it alive.
All in all I’m very happy with this: I’ve rebuilt an engine and it ran.
As I want the ignition independently isolated from the accessory electrics I’ve had to split the coil positive off at its join with the accessory circuit and wire it back in switched in series with that circuit.
The original 2CV fuse box uses glass fuses in a plastic case glued to the firewall at the back of the engine. As long as nothing goes wrong with it this works as well as it needs to but it’s not a solution you’d choose to keep if you were changing things.
As I’ve got a bare wiring loom for my Burton project, and I’ve done the hard work of identifying which connector is which, it was a relatively simple – if time consuming – task to replace each of the old glass fuse terminals with a female blade connector and cover them with an appropriately coloured piece of heat shrink. These then fit onto the male blade terminals of a generic after market fuse box.
Whilst there are only five fuses in a standard 2CV fuse box I’ve gone for eight as that gives me room to add fuses for some of the additional circuits I’m going to be adding – notably an electric fuel pump.
Whilst still not objectively easy, having a stripped wiring loom makes it significantly easier to identify which connector is which. To start with I’ll need the ignition and starter circuits so I can run the engine but having five holes in the wiring loom where the fuses are supposed to go makes figuring out what’s what more difficult than needs be.
So, after an evening probing around with a multimeter I’ve now identified both ends of all five fuses and which of those ends match up.
To make my life easier I have numbered them from 1 to 5:
- Instruments, indicator, wipers, alternator field (16A)
- Stop, interior and hazard lights (16A)
- Near side running lights (10A)
- Fog light (16A)
- Off side running lights (10A)
Next step will to be connect these up to a blade fuse box which will make life significantly easier and allow for fusing additional circuits.
After the initial de-clarting of the tinware I now moved on to trying to clean them up further. However, after the best part of a day (or what passes for daylight hours at this time of year) with various abrasives and power tools I’d not made much more than an impact on the surface.
As this has now sucked more than enough of my time I’ve opted to pay to have them sand blasted.
In the mean time I’ve picked up a new set of fixings to hold it all together when it’s done.
I’ve got some Dyane tinware for the Burton engine, this has the “back end of a horse power” forced induction take off and the cylinder covers are metal rather than whatever it is the later 2CVs used. However, it’s seen better days so needs some renovation.
First off the engine mounts needed removing with the aid of heat, Super Crack Ultra, and an impact driver. With that done I’ve declarted them using pound shop oven cleaner.
Next step will be to give them a thorough going over with various grades of abrasive.
I was doing a bit of tidying up work on the fuel tank which involves inserting some bolts vertically upwards. The problem with this – as I learned before – is that, under the influence of gravity, they will drop back into the socket which doesn’t leave enough thread protruding to bite into the nut.
Following the principle of the sump plug socket I put a slice of fuel hose into an 11mm socket.
The bolt now sits on top of the fuel hose with the full amount of thread available.
Although someone had painted the heads silver, the original rear wing retaining screws were rusty – to the point one had seized fast and had to be cut out when we took the wings off during the rechassis.
SPOG do replacement stainless screws for these so I picked up a pack.
As we’d done the hard work when we took the wings off, and had reassembled using copper grease, the old screws came out one at at time to be replaced with a new one.
As the rivnut at the bottom of the offside wing had been seized to the screw and had come out I used a flanged stainless nylock nut for that screw. (Standard M5 0.8 thread.)